Well,
this part of the work on the left rear quarter panel is kind of
anticlimactic………and that is actually a GOOD thing. Generally speaking, priming a body panel is a
relatively straight forward process and the success (or failure) of the primer
coat is largely determined by the amount of preparation you put into the panel
ahead of time.
As
I have documented over the last several weeks, a lot of time and effort has
been put into getting the left rear quarter as straight and clean as possible
before shooting the panel in epoxy primer/sealer. As the day approached to finally get the
panel in primer, I was checking and re-checking every detail to do as much as I
could to ensure success. And for the
most part, success is what I enjoyed.
However, as I have committed to tell the “whole” story on this blog, I
did have one relatively minor “oops” that caught me out that required a little
extra effort to fix and a second round of primer/sealer to get everything
straightened out.
On
the first “cut-in” shoot of all of the edges, wheel and window openings, I
queued up my small touch-up 3M PPS cup for the job. This cup is small and very maneuverable in
tight places and allows me to get primer in the detail areas quickly and
efficiently.
With
the cup full and the HVLP turbine spooled up, I started covering the cut-in
areas as quickly as I could to conserve primer and avoid excessive film
thickness. If I had been paying better
attention at this point, I would have recognized I was going through the primer
too fast to be normal and would have avoided a larger problem later. But, the signs of trouble were subtle enough
and I managed to get the cut-in work complete just as I ran out of primer, so
the brief window of enlightenment closed as quickly as it opened.
After
letting the cut-in work flash off for about an hour, I switched my gun over to
the large 3M PPS cup and started mixing up enough primer to coat the entire
quarter with a little bit of material to spare to catch any light spots I may
have missed. With everything checked
out, I started spraying from the bottom surfaces up, trying to move quickly
enough to avoid applying to much material.
Ya…….that’s how it SHOULD have worked anyway.
After
getting the full coat of primer on the panel, I noticed again how much material
I seemed to be using and how much more overspray I seemed to have (which is
very rare when using a turbine HVLP spray system). As I started quickly inspecting the freshly
coated surface, I began to notice very small sags in the primer at almost every
spot where the gun had been triggered or where each pass had overlapped. What the…..?????!!!!
Then
I decided to calm down and give this a “think” for a while and start
documenting every tiny detail that may have been out of the ordinary. After all, the primer was already on the
surface and the best thing I could do at this point was let it dry fully before
I could do anything remedial. So, with
that, I started my review of every detail.
Pretty
soon, I was confident that absolutely everything up to the actual process of
spraying the first cut-in coat was as perfect as I could make it. However, the first subtle hint of an issue
manifested itself in a slight “catch” in the trigger pull of the spray gun
while adjusting the spray pattern. While
an almost imperceptible difference in the gun, this small detail would
ultimately prove to be the single item that caused the domino-effect of the
whole issue.
The
bottom line is that this “catch” was an indicator that the needle was not
seating fully into the spray nozzle as a result of debris and paint residue
collecting in an almost hidden area of the trigger assembly that is not
mentioned in the gun maintenance and cleaning instructions (and YES, I read
them!). The end result was a small amount
of material was flowing through the gun all the time, so even when the gun was
not triggered, primer was still flowing ever so slightly, and thereby adding
thickness to the base coat and causing several small sags and few runs as well
when all things flowed out.
So,
after sleeping on this discovery overnight, and given the fact that I wanted to
let the primer cure fully before going after the goofed spots with the DA, I
set about doing a complete teardown, cleaning, lube and reassembly of my trusty
spray gun. This allowed me to revise my maintenance
schedule based on these new discoveries to ensure I never have this problem
again.
A
few days of cure time on the primer had the scene set to start repairing the
problem areas with a combination of shaving and sanding with the DA and a small
hand block with 80 grit paper. The rest
of the panel was scuffed with medium Scotch Brite pads and everything was
cleaned thoroughly with prep solvent and then tacked off in preparation for
round 2 of the priming exercise.
In
my usual preparatory fashion, I checked off each “pre-flight” detail as I
always do with the extra sensitivity to gun condition firmly implanted into the
process. With all boxes checked and the
surface freshly masked, cleaned and tacked, I was ready to give it another go.
This
time, the gun performance was stunningly improved and the primer laid down very
nicely. In what seemed like only a few
minutes, I had the entire quarter finished and was involved in cleaning up the
gun. At this point I started to question
just how long and slow this particular problem had been developing? Had I been working “around” this issue for
months and just not noticed the deterioration in performance? Who knows?
At the end of the day, the left rear quarter looks great and I am moving
operations to the right rear quarter for the same treatment. Hopefully, without the speckle of drama.
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Prep work is complete and the bare metal surfaces are cleaned and ready for masking. |
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The roof was previously primed for protection and this required scuffing with 80-grit paper to prepare it for the primer blending process into the previously primed area. |
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This is a close-up of the bare metal surface I prefer when applying primer. Most of this surface is created with 80-grit discs on a DA with light pressure. |
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All masked up for the first round of priming.......or so I thought! |
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First step would be priming these "cut-in areas around the window, trunk, door and wheel openings. |
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Shake, shake, shake..........shake your primer! It really is the only way and this inexpensive pneumatic shaker is ridiculously handy. Get one! |
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Objective evaluation of this shot reveals the first hint of trouble: that surface is far too gloss and "wet" than it should be and is worse in some spots than others. |
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After the first coat was completed, I started noticing more little hints that things were not quite right. In this shot, the primer has flashed about one hour and it still shows some obviously wet areas that should have started to dull by now. Uh oh...
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Out comes my inspection light and my worst fears are confirmed. Patches of slight to moderate sagging are evident on several areas of the quarter. *Insert long string of colorful expletives here!*
Careful investigation would reveal a very subtle spray gun fault that was responsible for the entire issue. Yep......fixed that. |
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Even after a few days of cure time, the panel remains too glossy for a "normal" primer application. I have my work cut out for me, but a few days of careful shaving and sanding of the problem areas and a complete tune-up of my spray gun and we were ready to give it a proper go. |
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This image shows a much more agreeable coat of primer. Not nearly as glossy and heavy looking as on the first round and it's laying very flat and smooth. |
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From another angle, the finish is clearly superior to the first attempt. Funny how things go when your equipment is up to par! |
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After the masking was pulled following only a hour of flash time, the surface look great and is noticeably smoother than before. We got this! |
Great troubleshooting Sven, Don't know if I would have figured that one out. I would probably have just attributed it to my lack of paint skill.
ReplyDeleteThat was my default position as it was Grant! LOL! As painting has become somewhat infrequent over the winter, I was definitely a bit rusty, so that made me believe that I wasn't really "allowed" to suspect an equipment issue. Either way, had to share the good AND the bad!
DeleteFortunately you had discovered the issue early-on in the exterior panel work. If this flaw had happened on your floor panels and the like, they certainly won't be noticed. Worst case there, you wasted a bit of primer. Glad you got it sorted out though, it looks like you got the panel straightened up very nicely!
ReplyDeleteAbsolutely agree Alex. And now I know exactly what I am looking for ahead of time so I don't get caught out with this issue again! A little time to correct, a little loss of material, and a valuable lesson learned........I can work with that.
DeleteAh...the "pre-flight" checklist. I love it! That panel looks really good. The think I would be mumbling "colorful metaphors" over would be the $$$ of epoxy primer used as DP-40 ain't cheap. Scares me to think I'll end up with $800-$1,000 in materials before I get to the actual color. I may have to look into an HVLP turbine system. Another bite of the elephant digested.
ReplyDeleteYa know I throw in the aviation references just to entertain ya Dennis! LOL!
DeleteThanks for the comments and you can believe watching some fresh primer go to waste wasn't high on my enthusiasm list for that week!
Arghhhh....there just ain't anything easy about this stuff is there !?! All I wanted to do today is sandblast some small parts. 3 minutes into the job, I have no sand and very little air coming out the gun tip. An hour later, I finally find a small piece of ice lodged inside one of the quick disconnect fittings on the air hose. Water?!?!? I have a water separator on the compressor - where did this come from?!? Walk over to the compressor and open the petcock on the separator - draining a pint onto the floor. Those water separators work much better when they're not full of water. Ughhhhh......I'm going to take up golf and get less stress in my life. Glad you got it sorted out Sven - at least it didn't happen on the color coat...yikes...we would have had to talk you back off the ledge!!! :) On to the right side then!
ReplyDeleterj
Easy? No. Golf? A one-ball game if there ever was one! Eliminating water in compressed air lines? Now THAT is a challenge! This was one of the HUGE drivers behind me moving to turbine HVLP for all painting that I do RJ. Warm, filtered air at a constant delivery rate that I can take anywhere with ease and not have to drain a single water trap. No oil to cause fish-eyes and puts more paint on the part than on the floor. Gotta love it!
DeleteFor the record, I hate chasing compressor water issues and it seems that no matter how much $$$$ is spent, the problem always seems to find a way to jam itself back into the equation.
On to the right side!